998 Mini Compression Test Results

998 Mini Compression Test Results

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Ben Magoo

Original Poster:

547 posts

229 months

Thursday 21st June 2012
quotequote all
So...

Been having some running issues with the old Mini Magoo for a while frown

(1981 - 998cc, single HS4 on water heated manifold (not connected), pancake K&N (freshly cleaned and oiled), red non waxstat jet. Minispares RC40 exhaust system, points ignition (red sliding) and Lucas 101 coil - both recently replaced in the last 4-6 months)

She's been starting beautifully from cold, a little lumpy sometimes to start with but generally ok-ish although definately under powered!. Problem has been when she's hot - not wanting to idle and being a bugger to start when warm?

On the L2B run I noticed a 'small' crack in the LCB 'Y' pipe (across the top of the 'Y') which I think was heating the fuel in the float bowl?

I've since welded that and resealed the rest of the system for good measure - but sadly the issues persist! frown

Tonight I have checked for sparks, there are plenty and bright and blue etc. I have observed the fuel filling the glass filter nicely and checked the operation of the float valve. The dashpot moves freely and has oil - it's either 20/50 engine oil or 3in1? can't remember what I put in last time.

As a precaution I have compression tested her showing around 120psi +/-5psi across all four cylinders! Internally she is completely standard, showing no signs of scoring etc at 115,000 miles with a copper head gasket installed about a year ago.

Ultimately my questions are:

1: Is 120psi enough for a standard 998 of this ilk? (8.3/1 comp???)

2: Could my running issues be timing/distributor related coupled with the fact that the manifold crack may have been present when I last replaced the points, condenser and coil. I adjusted the timing at the same time. (set at around 8 degrees from memory)

Thanks in advance!

Ben M

Cooperman

4,428 posts

257 months

Thursday 21st June 2012
quotequote all
120 psi per cylinder does seem a bit low.
When you did the compression test were all the other plugs out and the throttle fully open whilst you cranked it over for a minimum of 5 seconds.

Ben Magoo

Original Poster:

547 posts

229 months

Thursday 21st June 2012
quotequote all
Cooperman said:
120 psi per cylinder does seem a bit low.
When you did the compression test were all the other plugs out and the throttle fully open whilst you cranked it over for a minimum of 5 seconds.
Ah ok, no plugs were out one at a time and throttle fully closed. Mmm should have googled before hand (muppet!) - will try again tomorrow! lol

Cooperman

4,428 posts

257 months

Friday 22nd June 2012
quotequote all
My guess is that with all plugs out, a fully charged battery and the throttle fully open you'll get around 180 psi. Let us know.

davepoth

29,395 posts

206 months

Friday 22nd June 2012
quotequote all
Have you tried a new condensor?

GTRMikie

872 posts

255 months

Friday 22nd June 2012
quotequote all
davepoth said:
Have you tried a new condensor?
Worth a try. I've had brand new condensers that have been cr*p!

Ben Magoo

Original Poster:

547 posts

229 months

Friday 22nd June 2012
quotequote all
GTRMikie said:
davepoth said:
Have you tried a new condensor?
Worth a try. I've had brand new condensers that have been cr*p!
I'm not fitting another condenser ever! Next time it fails she's having electronic ignition! I'm very confident the sparks are good.

Tested her again tonight, plugs out, full throttle - 125psi! Although it does sound like my compression tester is leaking!? I've calculated a turn over RPM of around 300rpm - the needle rises to 100psi then flicks to 125 in time with the rpm. I'm attempting to reseal the tester tonight for another go in the morning?!

Also is 180psi really what I sould be seeing? There's not a great deal of info on this that I can easily find - (I've been told a race spec 1500 Haybusa runs around 220psi, a Ford Eco Boost around 80psi and a calculation I found last night gives a max potential psi of 166???) Confused dot com!

nick1275

1,272 posts

177 months

Friday 22nd June 2012
quotequote all
GTRMikie said:
davepoth said:
Have you tried a new condensor?
Worth a try. I've had brand new condensers that have been cr*p!
snap

camelotr

570 posts

175 months

Saturday 23rd June 2012
quotequote all
Ben Magoo said:
I'm not fitting another condenser ever! Next time it fails she's having electronic ignition! I'm very confident the sparks are good.

Tested her again tonight, plugs out, full throttle - 125psi! Although it does sound like my compression tester is leaking!? I've calculated a turn over RPM of around 300rpm - the needle rises to 100psi then flicks to 125 in time with the rpm. I'm attempting to reseal the tester tonight for another go in the morning?!

Also is 180psi really what I sould be seeing? There's not a great deal of info on this that I can easily find - (I've been told a race spec 1500 Haybusa runs around 220psi, a Ford Eco Boost around 80psi and a calculation I found last night gives a max potential psi of 166???) Confused dot com!
The "compression testing" (which is actualy a cylinder peak pressure test) is not realy able to give stabile measurements, which can be compared to "factory standards". We usualy use cheap gauges which read erraticaly, the measured amount is dependant on the camshaft, cranking speed, oil type, temperature etc.

The compression test is only good to compare the cylinders to each other. They should more-or less read the same if ok.

A much better way to test an engine is to complete a leak-down test. This will reveal the problems better.

Ben Magoo

Original Poster:

547 posts

229 months

Wednesday 27th June 2012
quotequote all
Yep got tired of trying to be clever so I took her to bits for the sake of 30mins to get the head off.

Here's how she looked as the head came off:


27062012460 by Ben Magee Creative Arts, on Flickr

Down bore #3:


27062012456 by Ben Magee Creative Arts, on Flickr

How the head looked:


27062012461 by Ben Magee Creative Arts, on Flickr

Is it possible to tell if it's an unleaded head? I have it in my mind that the head is not the original - the casting says it's a CAM4810?:


27062012467 by Ben Magee Creative Arts, on Flickr

Oh and this is what I got off the magnet?:


27062012453 by Ben Magee Creative Arts, on Flickr

Got a strait edge along block and head, couldn't slide a 0.05mm (0.002") feeler between the rule and the head so I'm pretty confident she's flat!

???

Edited by Ben Magoo on Wednesday 27th June 22:48


Edited by Ben Magoo on Wednesday 27th June 22:50

guru_1071

2,768 posts

241 months

Thursday 28th June 2012
quotequote all
id say that 99% that is an unleaded head, you can just see the ring of the seat around the exhaust valve - its the inner ring clse to the valve you have to look for, the wider ring is just a machining mark in the head.

if you take the valve out you will know for sure as you will see the seat in the throat

Jon Brown

678 posts

191 months

Thursday 28th June 2012
quotequote all
I cant help with your questions, but if your interested i have a Cooper 12G295 unleaded head and also a Swift tune SW5 cam kit with Venier pulley (only covered a few thousand miles) for sale.

Ben Magoo

Original Poster:

547 posts

229 months

Thursday 28th June 2012
quotequote all
Jon Brown said:
I cant help with your questions, but if your interested i have a Cooper 12G295 unleaded head and also a Swift tune SW5 cam kit with Venier pulley (only covered a few thousand miles) for sale.
YHM Jon smile

Ben Magoo

Original Poster:

547 posts

229 months

Monday 2nd July 2012
quotequote all
Spent a good 3-4 hours over a few nights stripping the valves out etc. All seems ok - gone from this:


_MG_0476 by Ben Magee Creative Arts, on Flickr

With some cleaning and lapping to this:


_MG_0481 by Ben Magee Creative Arts, on Flickr

With an overall look of:


_MG_0485 by Ben Magee Creative Arts, on Flickr

Generally everything looks nice and consistent, the head and block are flat, valve gear appears fine?

Once back together I'm thinking timing issues with specific attention to vacume advance maybe???

Also what are peoples experiences with worn carb jets? My red, none waxstat is about 8 years old and has done over 20k?

FWDRacer

3,564 posts

231 months

Tuesday 3rd July 2012
quotequote all
Jon Brown said:
I cant help with your questions, but if your interested i have a Cooper 12G295 unleaded head and also a Swift tune SW5 cam kit with Venier pulley (only covered a few thousand miles) for sale.
You'll need to insert it to reliably run unleaded smile

Ben Magoo

Original Poster:

547 posts

229 months

Monday 9th July 2012
quotequote all
Lost my rag and burnt it out! (well, I wanted to tonight!)

Got it all back together - no go.

An exercise in futility (and for the dake of £3.99) I fitted a new condenser tonight.

No go.

At which point I spat my dummy out packed up and decided to play a game I could win! (The washing up)

Going to calm down and start again at the begining tomorrow - battery's on charge ready for some churning Tuesday evening.

She's being a complete fking bh at the moment and I don't know why! FRUSTRATED DOT COM! furiousrage

Ben Magoo

Original Poster:

547 posts

229 months

Saturday 14th July 2012
quotequote all
What am I missing?

Air filter is clean and freshly oiled, carb is clean and free flowing, fuel's getting through.

The head gasket is fresh, the valves and clear and lapped.

The plugs are sparking the points are clean and set, the timing hasn't moved.

The exhaust is fully sealed and good to go.

She just ain't firing? I get the odd cough but she don't want to fking go!?

What the fking hell and I missing???

Pooky67

577 posts

166 months

Saturday 14th July 2012
quotequote all
What have you checked in the carb? Float ok? Piston drop test? Needle straight? Jet pipe clean?

Ben Magoo

Original Poster:

547 posts

229 months

Sunday 15th July 2012
quotequote all
Pooky67 said:
What have you checked in the carb? Float ok? Piston drop test? Needle straight? Jet pipe clean?
Yep all checked, all working correctly!

Think I'm going to throw in the towel and take it in on Tuesday frown

guru_1071

2,768 posts

241 months

Monday 16th July 2012
quotequote all
did you reset the valve clerances?

plug lead order???